Wednesday, March 30, 2011
Hoppy Days Are Here Again
My hops came up and are growng nicely. This is year two for these rhyzomes. It should be a good year if early growth is an indication. These are my Cascades. Can you spot the homebrew? Hint: It's an Irish Red. This is my Centennial. You'll note that it is smaller than the Cascade; last year it didn't produce any cones. I'm hopeful that it will produce in its 2nd year. Can you spot the homebrew? Hint: Its a freshly tapped Two Hearted Ale made with 100% Centennial hops. Someone on the west coast who drives a VW should be drooling...
Saturday, February 5, 2011
My New Mash Tun
I decided I needed a bigger mash tun. The 5 gallon round cooler I have been using for years just didn’t allow enough freeboard for brewing bigger beers, like the Brooklyn Brewery Black Chocolate Stout I made last October. I thought I would never get the sparge to run to completion on that one, and there was a lot of frustration involved in brew day because of it. BTW – the beer turned out fantastic – it will be my entry in the AHA competition this year if I don’t drink it all first.
So back on the ranch, I decided to double my capacity to a 10 gallon round cooler. It provides more than enough headroom for my 5 gallon brew day, even for big beers. Even super big beers. But I needed a replacement for the false bottom I have been using on my 5 gallon model. Because I am reluctant to spend money on things I think I can make myself, I decided to make my own.
Reflecting on some reading I have done on homemade mash tuns using rectangular coolers with copper pipe strainers, I figured the copper pipe concept would be adaptable to a round cooler as well. Using 1/2 inch copper pipe, tees, and elbows I made a three legged device that slipped inside of the 13 inch diameter cooler. I used an electric grinder with a thin cut off blade to make slices in the pipe at 3/8 inch intervals. I was careful to not cut too deep so as to weaken the pipe significantly and cause it to bend under the weight of a huge mash bill. I did minimal filing and cleanup to remove copper burrs.
I used the bung from my old unit to replace the plastic cooler valve, and pushed my hose through it into the waiting open tee inlet on the new copper header. The ID of the bung is slightly smaller than the OD of the hose, so it makes a good seal and didn’t leak a single drop of wort. The hose slipped into the copper tee with a wee bit of clearance but I figured what the hey, that’s just like cutting another slot in the copper pipe. I slipped some thick washers over the copper pipe to hold the device about 1/2 inch off of the cooler bottom. You can see in the picture that I actually introduced my mash water directly from the boil kettle through the device into the BOTTOM of the mash. No guessing on when I had enough mash water!
All of the parts (8 pipes, 4 elbows, and 3 tees) slip together and are easily disassembled for cleaning, drying and storage.
The device worked great! I was concerned that I might not get enough flow out of the slots I cut (I actually did calculate the total flow area) but I ended up having to restrict the flow from the hose in order to sparge at a reasonably slow flow rate. You can see from the photo that there was plenty of headroom after mashing with this 12 pound grain bill. I need to adjust my calculations on strike water temperature a bit to allow for the different heat transfer properties of the larger cooler.
By the way, the beer I made was Bell’s Two Hearted Ale, one of my favorite IPAs. I’m thinking of using it for Brett bait. I brewed it on January 29, 2011, which would have been my grandma’s 100th birthday had she still been alive. I’m going to have to come up with a catchy name for it to commemorate that special event. The original gravity came in at 1.062, and I just measured a 1.014, so I’m looking at a 6.5 percenter or better. The bitterness and the flavor of the 100 percent Centennial hops was excellent! I’m going to let the beer rest on the cold yeast (56 degrees right now and I’m trying to keep it warmer in our current cold spell) for another week to assure minimal diacetyl, then I’ll rack to secondary and dry hop and let it condition cold for a couple of months.
Until next brew day (which probably won’t be until April due to a heavy day job work load), Cheers!
So back on the ranch, I decided to double my capacity to a 10 gallon round cooler. It provides more than enough headroom for my 5 gallon brew day, even for big beers. Even super big beers. But I needed a replacement for the false bottom I have been using on my 5 gallon model. Because I am reluctant to spend money on things I think I can make myself, I decided to make my own.
Reflecting on some reading I have done on homemade mash tuns using rectangular coolers with copper pipe strainers, I figured the copper pipe concept would be adaptable to a round cooler as well. Using 1/2 inch copper pipe, tees, and elbows I made a three legged device that slipped inside of the 13 inch diameter cooler. I used an electric grinder with a thin cut off blade to make slices in the pipe at 3/8 inch intervals. I was careful to not cut too deep so as to weaken the pipe significantly and cause it to bend under the weight of a huge mash bill. I did minimal filing and cleanup to remove copper burrs.
I used the bung from my old unit to replace the plastic cooler valve, and pushed my hose through it into the waiting open tee inlet on the new copper header. The ID of the bung is slightly smaller than the OD of the hose, so it makes a good seal and didn’t leak a single drop of wort. The hose slipped into the copper tee with a wee bit of clearance but I figured what the hey, that’s just like cutting another slot in the copper pipe. I slipped some thick washers over the copper pipe to hold the device about 1/2 inch off of the cooler bottom. You can see in the picture that I actually introduced my mash water directly from the boil kettle through the device into the BOTTOM of the mash. No guessing on when I had enough mash water!
All of the parts (8 pipes, 4 elbows, and 3 tees) slip together and are easily disassembled for cleaning, drying and storage.
The device worked great! I was concerned that I might not get enough flow out of the slots I cut (I actually did calculate the total flow area) but I ended up having to restrict the flow from the hose in order to sparge at a reasonably slow flow rate. You can see from the photo that there was plenty of headroom after mashing with this 12 pound grain bill. I need to adjust my calculations on strike water temperature a bit to allow for the different heat transfer properties of the larger cooler.
By the way, the beer I made was Bell’s Two Hearted Ale, one of my favorite IPAs. I’m thinking of using it for Brett bait. I brewed it on January 29, 2011, which would have been my grandma’s 100th birthday had she still been alive. I’m going to have to come up with a catchy name for it to commemorate that special event. The original gravity came in at 1.062, and I just measured a 1.014, so I’m looking at a 6.5 percenter or better. The bitterness and the flavor of the 100 percent Centennial hops was excellent! I’m going to let the beer rest on the cold yeast (56 degrees right now and I’m trying to keep it warmer in our current cold spell) for another week to assure minimal diacetyl, then I’ll rack to secondary and dry hop and let it condition cold for a couple of months.
Until next brew day (which probably won’t be until April due to a heavy day job work load), Cheers!
Monday, November 1, 2010
Celebrating Something
I made a batch of Celebration Ale this weekend. I always make a batch of beer when one of my younguns is soon to have a baby. Recent batches have included Wait for Nate (which surprisingly turned into Ain't Nate) and Hey Jude Celebration Ale. Since I don't have the predetermined name of the baby yet, I can't name the beer. For now I'll just name it Yummy Beer. It's a perennial favorite that I make every year for the Holidays. This beer will also be ready in time for Dr. Beyer's arrival. The OG came in at 1.056 (a bit disappointing), but I'm hoping for good attenuation which may drive the final gravity to lower than expected levels and yield a bit more alcohol kick. I couldn't find any Safale US-05 yeast locally, so I went with a double pitch of Nottingham Ale Yeast. If you don't try different things, you'll never try different things, correct?
So stay tuned for details on the outcome. The beer and the baby...
So stay tuned for details on the outcome. The beer and the baby...
The Numbers Are In
The Black Chocolate Stout appears to have attenuated nicely. The starting gravity came in at 1.089, and the last check on the final gravity yielded a 1.019. My goals were 1.090 and 1.023, so not a bad effort. In terms of alcohol content, we should be looking at just over 9% ABV. Perfect for Dr. Beyer's visit at Christmas time. I've got in in the keg and am conditioning it for 6 more weeks before I partake. I've never been able to hold off that long on a batch; wish me strength.
I've been focusing on yeast performance as of late, especially since I detected diacetyl in my rye-wheat batch made over the summer. I'm lead to believe that petite mutants, those respiratory deficient little buggers with their impaired mitochondria, may have created the problem. I controlled the fermentation temps to lower levels, trying to maintain around 66 degrees for the first week, then slowly bringing it down to around 60 degrees before taking it off of the yeast cake. This, combined with a double sized pitch quantity from a healthy starter should do the trick for eliminating undesirable flavors. I also aerated the dickens out of the wort with my aquarium pump and stone.
Oh, did I say that it was BLACK chocolate stout. Check out my favorite coffee cup below. Hint: it ain't coffee in that cup.
I've been focusing on yeast performance as of late, especially since I detected diacetyl in my rye-wheat batch made over the summer. I'm lead to believe that petite mutants, those respiratory deficient little buggers with their impaired mitochondria, may have created the problem. I controlled the fermentation temps to lower levels, trying to maintain around 66 degrees for the first week, then slowly bringing it down to around 60 degrees before taking it off of the yeast cake. This, combined with a double sized pitch quantity from a healthy starter should do the trick for eliminating undesirable flavors. I also aerated the dickens out of the wort with my aquarium pump and stone.
Oh, did I say that it was BLACK chocolate stout. Check out my favorite coffee cup below. Hint: it ain't coffee in that cup.
Saturday, October 9, 2010
BIG Brew Today
Big brew day today…my buddy Jack is in from Spokane and we’re going to do a very large American Stout; a clone of Brooklyn Brewery Black Chocolate Stout – one of my perennial favorites. Too bad Andy isn’t here…he used to be pretty good at this.
Here’s the grain bill:
15.5 lbs pale
1 lb chocolate
¾ lb white wheat
½ lb roasted black barley
¼ lb flaked wheat
3 oz black patent
That equates to 18 plus lbs of grain. Yeah baby! We’re looking for an OG of 1.090 plus! If I can bring her down to a target 1.023 FG, she should come in at 9% ABV with good attenuation.
I’m going to mash in at 154 degrees to get some extra sweetness and mouthfeel. This should be a very large beer suitable for drinking in January on these bitterly cold southwest Louisiana nights:)
Here’s the hops bill:
2 oz Kent Golding 60 min
½ oz Amarillo and ½ oz Kent Golding 15 min
½ oz Amarillo and ½ oz Glacier 5 min
The estimated IBU is 46. Did I ever mention that Garrett Oliver is one of my beer heroes?
I also made a yeast starter using Safale 05 dry yeast on Tuesday night / Wednesday morning to assure that there would be a sufficient quantity of the little buggers to address the high gravity wort head on!
Stay tuned for brew day details! There will also be stogies involved and endless college football. I only hope safety professional Jack can be of some assistance lifting these heavy containers…
Here’s the grain bill:
15.5 lbs pale
1 lb chocolate
¾ lb white wheat
½ lb roasted black barley
¼ lb flaked wheat
3 oz black patent
That equates to 18 plus lbs of grain. Yeah baby! We’re looking for an OG of 1.090 plus! If I can bring her down to a target 1.023 FG, she should come in at 9% ABV with good attenuation.
I’m going to mash in at 154 degrees to get some extra sweetness and mouthfeel. This should be a very large beer suitable for drinking in January on these bitterly cold southwest Louisiana nights:)
Here’s the hops bill:
2 oz Kent Golding 60 min
½ oz Amarillo and ½ oz Kent Golding 15 min
½ oz Amarillo and ½ oz Glacier 5 min
The estimated IBU is 46. Did I ever mention that Garrett Oliver is one of my beer heroes?
I also made a yeast starter using Safale 05 dry yeast on Tuesday night / Wednesday morning to assure that there would be a sufficient quantity of the little buggers to address the high gravity wort head on!
Stay tuned for brew day details! There will also be stogies involved and endless college football. I only hope safety professional Jack can be of some assistance lifting these heavy containers…
Saturday, October 2, 2010
My Boat Babe
I was drinking a homebrew on Friday night while preparing for a Saturday fishing trip and discovered this in my boat. Isn't she beautiful? I'm crazy about my boat babe...
Then, when I went to get a refill, I came back and the neighbors were in my boat.
Then, when I went to get a refill, I came back and the neighbors were in my boat.
We had good Friday night...
Subscribe to:
Posts (Atom)